Porosity in Aluminum Engine Block


Porosity in Aluminum Alloy Die-Casting Engine Blocks: Causes and Solutions

Porosity Formation Principles

Porosity in aluminum alloy die castings falls into two types: precipitation porosity and entrapped porosity. Precipitation porosity arises from high melting temperatures (>750°C) increasing hydrogen solubility in the melt, or from slag-heavy revert material with poor deslagging. Entrapped porosity stems from process or design flaws, such as low shot sleeve fill ratios, premature high-speed injection, excessive mold release agent gas, or poorly designed gating and venting systems, trapping gas in the melt. These pores are typically smooth-walled and round, appearing at casting ends or complex areas.

Porosity Formation Diagram
Alt: Diagram illustrating precipitation and entrapped porosity formation in aluminum alloy die casting.

Problem Description

An 8.5kg ZL201 aluminum alloy engine block, cast on a Buhler 28,000kN cold-chamber machine, showed random porosity on its marking surface via X-ray and machining checks. In 2017, the porosity rejection rate hit 2.5%, with smooth, dark gray pores threatening sealing and strength—unacceptable per technical specs.

Porosity Distribution on Marking Surface
Alt: X-ray image showing porosity distribution on the engine block marking surface.

Solution Approach

Porosity results from melt quality, process parameters, and mold design. Precipitation porosity can be curbed by refining melting practices, while entrapped porosity ties to filling dynamics. The strategy involved tackling process settings, melt purity, and gating design step-by-step to pinpoint and eliminate key causes.

Solution Methods

Process Parameter Adjustments

Issue: High-speed injection started at 500mm (reasonable), but complex cavities trapped gas; post-spray mold temperature was 120°C—below the ideal 160-190°C—causing excess release agent gas.
Fix: Delayed high-speed start to 510mm, reduced spray time from 1.5s to 1s, and added 0.5s air blow, raising mold temperature to 160°C.
Result: Rejection rate dropped from 2.5% to 2.3%—modest progress.

Melt Process Optimization

Issue: Revert material exceeded 50% with poor cleanliness, raising hydrogen content (density 1.523).
Fix: Pre-dried revert limited to 30%-45%, degassing time extended from 260s to 300s.
Result: Hydrogen density fell to 0.927, reducing rejection rate to 2%—still insufficient.

Gating System Improvements

Issue: Gating design caused turbulent filling and gas entrapment at the marking surface (Figure 3).
Fix: Mold flow analysis guided changes: sealed Gate 1, widened Gate 2 by 3mm, narrowed Gate 3 by 3mm.
Result: Improved filling eliminated entrapment (Figure 4), cutting marking surface rejection rate to 0.12%.

Mold Flow Analysis of Gating System
Alt: Mold flow analysis showing optimized melt filling sequence after gating adjustments.
X-Ray Comparison Before and After
Alt: X-ray comparison of porosity on the marking surface before and after improvements.

Improvement Summary Table

StageIssue IdentifiedAction TakenRejection Rate
Process ParametersEarly high-speed, low mold tempDelayed start, adjusted spray/blow2.5% → 2.3%
Melt OptimizationHigh hydrogen in meltCleaner revert, longer degassing2.3% → 2.0%
Gating RedesignTurbulent fillingSealed Gate 1, resized Gates 2 & 32.0% → 0.12%

Conclusion

Porosity in the engine block arose from hydrogen in the melt and gas entrapment during filling. Initial tweaks to process and melt reduced defects modestly, but gating redesign via mold flow analysis proved decisive, slashing the rejection rate from 2.5% to 0.12%. This step-wise approach offers a practical blueprint for tackling similar porosity issues in die casting.

Shawn Avatar

I’m Shawn, a dad to a lively 2-year-old and a native of a scenic Three Gorges town. My journey as a consumer electronics KA led me to YuGe, where I’ve witnessed bold ideas become star products. Through this blog, I share insights and real-world cases in consumer-grade die-casting, hoping to inspire and grow together!